AirSpeed VW Community Forums
General Forums => Air Speed Lounge => Topic started by: Boost_Retard on July 03, 2004, 12:10:08 PM
-
it sucks that the races were shut down yesterday..but it gave me lots more time to get my car done right.. Just thought i would update..
all the gauges are in...hooking up the oil sending unit now..finally after 5 trips 2 lordco i got two new fuel filters that are exactly what came out of my car, 18 bucks each!
and in the fuel filter i pulled out..i found a big booger..looks like silicone that fell in while changing sending unit on tank..dont ask... :(
put in new MSD wires and plugs.
cutting SS braid oil lines now.. gonna have them all done in a few hours.
then a windsheild change and im good 2 go.
im SURE its going 2 work now..it has 2 or else!
filled her up with some 110octane..gonna try a some more boost if its running right!
Cale
-
see you at A&W tomorrow then
-
Well it looks like i jumped the gun again..
things are not looking SO good after all...sure the car runs fine now (well it seemed that way on my 30 second drive) but i cant get more then 25 oil PSI..tried 2 gauges..with 2 different power supplys..
i did however get an oil psi booster kit from air speed today. (thanx for leaving that out for me!)
Altho i think it will do little to fix my problem..
I dont know if a plugged up oil filter in a full flow system could cause this low oil PSI problem..but i have a funny feeling that some weird snot has built up in the filter..if not that..it must be a pick up tube problem..
motor does not leak a drop..and never has..maybe the low oil PSI is why!
im gonna tear most of the motor apart tommrow to figure this NEW problem out..ohh joy.
Cale